As a result, Gulfstream is not responsible or liable for your use of any materials or information obtained from this site.The National Transportation Safety Board determined that the captain of Colgan Air flight inappropriately responded to the activation of the stick shaker, which led to an aerodynamic stall from which the airplane did not recover.

Contributing to the accident were (1) the flight crew's failure to monitor airspeed in relation to the rising position of the low-speed cue, (2) the flight crew's failure to adhere to To state that fatigue was a contributing factor, and thus part of the probable cause, would be inconsistent with the above finding and would, therefore, disrupt this flow of logic. On February 12, , a Colgan Air, Inc.

The current air carrier approach-to-stall training did not fully prepare the flight crew for an unexpected stall in the Q400 and did not address the actions that are needed to recover from a fully developed stall.Those findings were immediately followed by the Board's "Probable Cause" statement: The NTSB could not explain why the first officer retracted the flaps and suggested that the landing gear should also be retracted, though it did find that the current approach-stall training was not adequate: Accident Report Loss of Control on Approach, Colgan Air, Inc., Operating as Continental Connection Flight 3407, Bombardier DHC-8-400, N200WQ, Clarence Center, New York, February 12, 2009 by National Transportation Safety Board. Colgan Air Flight 3407, marketed as Continental Connection under a codeshare agreement with Continental Airlines, was a scheduled passenger flight from Newark, New Jersey, to Buffalo, New York, which crashed on Thursday, February 12, 2009.The aircraft, a Bombardier Dash-8 Q400, entered an aerodynamic stall from which it did not recover and crashed into a house in Clarence Center, New … Data extracted from the FDR revealed the aircraft went through severe Freezing temperatures made it difficult to access crash debris. Pilot error was one of the chief causes that led to the deadly crash of Colgan Air flight, operating as Continental Connection Flight , last February, federal investigators said today. COLGAN Air CRASH Flight 3407 Continental Connection Bombardier Dash-8 Q400 2009 NTSB ATC Audio. Always remember that Eddie, when you get right down to it, is just a pilot. The NTSB could not explain why the first officer retracted the flaps and suggested that the landing gear should also be retracted, though it did find that the current approach-stall training was not adequate:The current air carrier approach-to-stall training did not fully prepare the flight crew for an unexpected stall in the Q400 and did not address the actions that are needed to recover from a fully developed stall.Those findings were immediately followed by the Board's "Probable Cause" statement:The captain's inappropriate response to the activation of the stick shaker, which led to an aerodynamic stall from which the airplane did not recover. Zero Hours_ Swissair Flight 111 plane crash (Fire in the Cockpit Disaster ) Crime Watch. The cockpit had sustained the greatest impact force, while the main cabin was mostly destroyed by the ensuing fire. Contributing to the accident were (1) the flight crew's failure to monitor airspeed in relation to the rising position of the low-speed cue, (2) the flight crew's failure to adhere to To state that fatigue was a contributing factor, and thus part of the probable cause, would be inconsistent with the above finding and would, therefore, disrupt this flow of logic.